Journal of Chongqing Jiaotong University(Natural Science) ›› 1998, Vol. 17 ›› Issue (1): 92-95.
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Li haohong1
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黎绍泓1
作者简介:
Abstract: Huaxi Lock in the Lianjiang River has been in operation for more than twenty years. The set tlements occurred in the lower head of the lock, though in different degrees, are maialy due to the failure of solution caverns under the foundation, and foundation erosion. The pressure grounting technique for the foundation of lower head, and concrete floor placing method for the chamber are used in order to increase foundation bearing capacity and impermeabicity. The methods proved to be effective.
Key words: lower head, foundation, grounting, reinforcement, seepage control
摘要: 已运转20余年的连江花溪船闸, 因下闸首地基溶洞压穿, 地基冲刷造成下闸首出现不均匀沉陷.为此, 采用下闸首地基压力灌浆和闸室浇筑混凝土底板的办法, 提高地基承载能力和抗渗能力, 取得良好效果.
关键词: 下闸首, 地基, 注浆, 加固, 防渗
CLC Number:
U641
Li haohong. Treatment of Karst Foundation of the Lower Head of Huaxi Lock in the Lianjiang River[J]. Journal of Chongqing Jiaotong University(Natural Science), 1998, 17(1): 92-95.
黎绍泓. 连江花溪船闸下闸首地基岩溶处理工程[J]. 重庆交通大学学报(自然科学版), 1998, 17(1): 92-95.
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